Shreddinlettuce
Well-Known Member
- Joined
- Nov 20, 2016
- Location
- Hickory
I hear he likes rearends…Oh man, please don't bring your sex life into my build thread![]()
Are you gonna run some kind of uhmw or anything on the skid?
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I hear he likes rearends…Oh man, please don't bring your sex life into my build thread![]()
I hear he likes rearends…
Are you gonna run some kind of uhmw or anything on the skid?
I think the AR500 slides better than UHMW. It tends to dig and gouge where the AR500 just glides and slides.1/2" UHMW is the plan I think, problem is the skid is AR500 so you not drilling and tapping it
Looks like the paint department failed to cover up that weld porosity, should’ve used truck bed linerThings that make you go
WTF At max droop there is 1/4" clearance. Why remove so much material when not necessary
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Supposed professional driveshaft shop built the shafts. I'm no great welder but damn, just damn.....
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More dumdfuckery to unfuck...... maybe I'm just too OCD![]()
I think the AR500 slides better than UHMW. It tends to dig and gouge where the AR500 just glides and slides.
it definitely does, I wouldnt add UHMW underneath that AR500, let it ride.
How thick is the material? If its at least 3/16 I would just run your tube supports in the belly up against the back of the AR and let it be. If you really want a thicker belly pan, you can back the AR with some mild steel, but its not really necessary, that AR plate is incredibly strong
oh yea I wouldnt bother at all with any UHMW. You wont tear that AR plate up.It's 1/4" and the plan was to run two support tubes
The carrier bearing has been relocated at some point about ~2" upward. This gives a ~13° angle between the two shafts at full droop. You can see the original lower mounting holes. I would need to cut a slot in the secondary plate that was added to lower it so I can't easily check the angle. However from my calibrated eyeball, it would position the the shafts close to zero at full droop. In the current position at ride height the shafts would have minimal angle which is more ideal. Judging from the quality of the welds this was done by BTF during the original build. Unless I'm missing something I'm going to leave the bearing in the upper location for now.
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@partiallycommittedracing thoughts?
Barnes sells these in 4 thread sizes for $2 s piece if you’re lucky to need one of those sizes.
Barnes sells these in 4 thread sizes for $2 s piece if you’re lucky to need one of those sizes.
But simple parts on a lathe are fun to make
@Andy J. sell him some good cutting tools!I've been beveling material with a pneumatic beveler for years. A few months ago I bought a DeWalt cordless router and have been using it with carbide wood bit to bevel aluminum and it works well. I have been seeing ads for Dirt Church Industries carbide beveler that uses replaceable carbide bits and thought it looked cool. They recently released a small table that fits DeWalt and Milwaukee cordless routers. Combo table and bit was like $160 I think. We'll see how it works
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Holy beef Batman!Skid plate and subframe completed. Added some reinforcements to the front that connects to the subframe. With the suggestion of @partiallycommittedracing I added a couple of rear support bars. The subframe bolts in place so it's easily removed for service. I had 1.5' tube clamps but they were the interlocking style which can be a PITA and they also only use 5/16" bolts. Spent way too much time making some the way I wanted themWelded, cleaned up, and ready for paint.
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Holy beef Batman!

#racecarshitJust like when you strap something down on a trailer and say "That ainty going anywhere"...."That shit ain't gonna bend"![]()
looks badass! gonna be great to see this thing back on the trails!Skid plate and subframe completed. Added some reinforcements to the front that connects to the subframe. With the suggestion of @partiallycommittedracing I added a couple of rear support bars. The subframe bolts in place so it's easily removed for service. I had 1.5' tube clamps but they were the interlocking style which can be a PITA and they also only use 5/16" bolts. Spent way too much time making some the way I wanted themWelded, cleaned up, and ready for paint.
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Just like when you strap something down on a trailer and say "That ain't going anywhere"...."That shit ain't gonna bend"![]()