- Joined
- Jan 3, 2015
- Location
- Boone NC
TOO LATE...and yes i've done it before timing and all but money is tight for all that work. forgot to mention i was pulling plug to do "leak down test" as my final test on it before putting all new coils on just to make sure that test passes along with other tests i've done and here i am. doing head/timing jobs is nothing new to me i just can't afford it and i'm not one to pull just one head and replace one gasket but reuse timing and stuff..kinda pointless unless a absolute must have to
heli coil is screwed all to pieces. put camera down in there cylinder looks fine, all the valves look good (surprisingly clean for mileage), but the #4 is pretty buggered up so i redone a new bigger heli coil with TONS of Red thread-locker and hope for the best cause either way if this don't hold up, the head is no good anyways so figured might as well lock it down all the way LOL. finished putting it back together with all new gaskets from lower intake up, all new coils, new knock sensor while there and replaced the CHT censor too and so far runs good but i just let it idle and drove down the road and back. tomorrow gonna take it on a drive and see how it does. (i guess time to start looking for another set of heads or motor..whichever deal comes the best). at least i know this heli coil ain't going nowhere..hehe but doesn't guarantee it won't ark later on and start missing but keeping my hopes high on it. (a rubber hose jammed on the plug and twisting it while pulling up got it to catch the rest of the threads and came right out after another 5 or 6 turns). thanks for all you guys help.
LOL.
